From 7d86ccce037b50caa0f12b57b5f45dc7d512d72b Mon Sep 17 00:00:00 2001 From: Daniel Schaefer Date: Thu, 19 Jan 2023 11:47:48 +0800 Subject: [PATCH] lotus: Fix BOOT_DONE Must be pulled low when we're done. Signed-off-by: Daniel Schaefer --- keyboards/lotus/lotus.c | 2 +- 1 file changed, 1 insertion(+), 1 deletion(-) diff --git a/keyboards/lotus/lotus.c b/keyboards/lotus/lotus.c index c6f07c6d65..5b2e321f1d 100644 --- a/keyboards/lotus/lotus.c +++ b/keyboards/lotus/lotus.c @@ -67,7 +67,7 @@ void keyboard_pre_init_kb(void) { // Before this, when holding down both alt keys QSPI_SS is pulled low to put // the RP2040 in bootloader mode during reset. setPinOutput(BOOT_DONE_GPIO); - writePinHigh(BOOT_DONE_GPIO); + writePinLow(BOOT_DONE_GPIO); //// TODO: Do we ever need to disable it to save power? setPinOutput(MUX_ENABLE_GPIO);